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Ultimate cost reduction! Iron smelting plant focus on hot metal homogeneous silicon index optimization, small adjustments leverage large cost reduction!

"The things of the world are often accomplished through diligence and frugality rather than extravagance." In today's competitive market environment, reducing cost and increasing efficiency has become the core password of enterprise survival and development, and it is the only way to enhance competitiveness and achieve sustainable development. Hebei Xinda Group deeply insight into this trend, for many years to unswervingly implement the cost reduction and efficiency strategy, group companies to optimize the process flow, improve operating methods, etc., to reduce cost and increase efficiency work into a strong impetus.

Hebei Xinda Iron and Steel Group Co., Ltd. steelmaking plant follows the banner of cost reduction and efficiency, strives to sharpen its own potential, vigorously carries out cost reduction work, and makes positive contributions to the achievement of business objectives. Recently, the ironmaking plant has compared the silicon homogenization value of the blast furnace with that of other blast furnaces in the company and found that it is high, and the silicon control is more conservative under the premise of eating economic materials. In order to achieve the goal of stable production, coke saving and high quality, and reduce the production cost and ton iron cost, the ironmaking plant has set up a lean improvement group to carry out the research on the reduction of hot metal silicon in blast furnaces.

In the process of focusing on reducing the value of hot metal parsimony, the lean improvement team of the ironworks carefully made a cause analysis chart, from the production impact and reduction mechanism and way, a comprehensive analysis of various factors affecting hot metal parsimony, and by checking the functional unit reports, formulating operating policies, checking the blast furnace daily and iron-making reports, blast furnace operating curves and other means. Finally, four main reasons were determined: iron rhythm, manganese content in molten iron, basicity of slag and top pressure of furnace.

After clarifying many factors affecting hot metal homogeneous silicon, the research team acted quickly and developed a series of effective improvement measures. In view of the reason that the iron production rhythm is not compact, the iron production rhythm is strengthened, the smelting intensity and utilization coefficient are improved, the contact time between iron drops and ash in coke is reduced, and the time of iron drops passing through the blast furnace layer is also reduced, and the silicon entering the hot metal will be reduced. Organize the iron opening of the field in advance, zero interval organization, which can avoid the iron interval exceeding the specified time due to organizational problems.

Aiming at the cause of low manganese content in hot metal, by adding ore blocks with high manganese content or increasing the proportion of ore blocks with high manganese content, under the premise of not affecting the burnup level of blast furnace, iron ore blocks and Mb blocks with high manganese content are appropriately increased to increase the manganese content in hot metal, which can improve the fluidity of slag and iron and reduce the cost of raw materials.

In view of the reasons for the low basicity of slag, timely check the composition of incoming ore, improve the proportion of incoming sinter, and ensure that the alkalinity is controlled within a reasonable range. To this end, the research team has re-formulated the battering accounting system, which is different from the previous adjustment of binary alkalinity, such as Si and S exceeding the specified value, and the calculation of alkalinity is checked every hour, and the alkalinity is checked according to the difference of the composition of adjacent hot metal △Si and △S. Thus, the sulfur content of molten iron has a higher internal control rate while ensuring the reduction of silicon.

In view of the reasons for the low top pressure, the research team decided to first increase the inlet air volume, activate the furnace cylinder, and then gradually increase the top pressure setting value to ensure that the top pressure is in the safe range to avoid damage to the top equipment.

After unremitting efforts and research, after strictly implementing a series of carefully formulated improvement measures, the value of homogeneous silicon in hot metal has been effectively controlled. In the improvement process, not only the economic material has stabilized the furnace condition, but also the improvement of various economic and technical indicators, and the concept of cost reduction and efficiency has been effectively implemented, but also the establishment of technical operating procedures and operation instructions for the post, so that the staff have rules to follow in their daily work.

Xinda people uphold the concept of diligence and frugality, actively change and innovation, from the rational use of office supplies to the fine control of the production link, in-depth mining of every potential, continuous optimization, bit by bit convergence into a significant cost advantage. Looking into the future, cost reduction and efficiency increase are still the indispensable core of enterprise development strategy. Xinda people should continue to adhere to diligence and thrift, with the fearless spirit of exploration, unswervingly increase technology research, comprehensively improve production efficiency, reduce production costs, courageously move forward toward the goal of creating an excellent enterprise, and work together to innovate brilliant!

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